Hydrocarbons

A major LPG explosion and subsequent fire occurred at the Conoco Humber Refinery (now Phillips 66) in the Saturate Gas Plant (SGP) area.The incident was initiated by the catastrophic failure of an overhead pipe carrying flammable hydrocarbon vapours from the de-ethaniser column. ÂThis released a large vapour cloud which ignited, causing a significant explosion and a fire that burned for over three hours, severely damaging the SGP and surrounding units.

Date
16/04/2001
Location
United Kingdom
Industry
Energy (Oil Refining)
Substance
Hydrocarbons
Cause

The immediate cause was the catastrophic rupture of a 6-inch diameter carbon steel pipe elbow (Line P4363) in the de-ethaniser overheads circuit. This failure resulted from severe internal erosion-corrosion. A water injection point, added years earlier to prevent downstream fouling but located just 67cm upstream of the elbow without a proper dispersion device, continuously washed away the protective internal iron sulphide layer. This allowed corrosive agents in the stream (H2S, chlorides etc.) to aggressively attack the exposed pipe wall, reducing its thickness from ~7.1mm to as little as 0.3mm in places. Root causes identified by the Health and Safety Executive (HSE) investigation included: Â

  • Inadequate Pipework Inspection Regime: The refinery’s inspection system failed to identify the severely corroded state of the pipework.
  • Insufficient Management of Change (MoC): The potential impact of installing and operating the water wash point on upstream pipework integrity was not adequately assessed or managed.
  • Weaknesses in Corrosion Management: Systems and resources for identifying, assessing, and mitigating corrosion threats (particularly location-specific ones like downstream of injection points) were insufficient.
Consequence
  • Large Vapour Cloud Explosion (VCE) followed by a major fire lasting over 3 hours. Â
  • Extensive damage leading to the write-off of the Saturate Gas Plant (SGP).
  • Significant damage to adjacent units (e.g., Coker closed blowdown system) and widespread lesser damage across the site, including administration buildings, canteens, and stores (damaged cladding, glazing, minor structural damage).
  • Damage to off-site properties (mainly broken windows, some minor structural damage) up to 1.5km away in South Killingholme and Immingham, with 370 separate damage reports received.
  • Temporary shutdown of the entire refinery operations.
  • Release of asbestos due to damage to lagging materials.
  • Minor injuries on site; remarkably few considering the scale, attributed to it being a Bank Holiday with reduced staffing (~185 on site vs. ~800 normally) and timing near shift change.
Injuries

1 minor on-site injury and 2 minor off-site injuries

(Note: An IChemE paper notes 71 subsequent civil claims for injury were pursued by workers and members of the public.)

Fatalities
N/A
Lessons Learned
  • Mechanical Integrity: The critical need for robust, risk-based inspection (RBI) programs for pipework that specifically address potential degradation mechanisms (like erosion-corrosion) and identify high-risk locations (e.g., downstream of injection points).
  • Management of Change (MoC): Rigorous assessment of all process and plant modifications is essential to identify and mitigate potential unintended consequences, including impacts on material degradation.
  • Corrosion Management: Effective corrosion management requires dedicated systems, expertise, sustained resources, and clear communication to ensure potential threats are understood and controlled throughout the plant lifecycle. Understanding the interaction between process fluids, materials, and operating conditions (including additions like water wash) is crucial.
  • Hazard Identification: Recognising and assessing specific hazards introduced by operational practices or modifications is vital for prevention.
Sources / References
  1. Health and Safety Executive (HSE). “Public report of the fire and explosion at the ConocoPhillips Humber refinery on 16 April 2001.”
  2. Carter, J., Dawson, P., Nixon, R. “Explosion at the Conoco Humber Refinery – 16th April 2001.” IChemE Loss Prevention Bulletin, 151 (2006).Â
  3. ARIA (Analyse, Recherche et Information sur les Accidents), French Ministry of Environment accident database. Summary report 20541_en.Â
  4. IChemE Safety & Loss Prevention Special Interest Group. Incident Summary: “Deethaniser Overhead Line Rupture”.
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Analysis

  • The sequence of events on 16th April 2001 unfolded rapidly. Prior to the incident, the SGP unit was reported to be operating normally with no recent process upsets. Unbeknownst to the operators, the critical elbow in pipe P4363 was severely weakened. At approximately 14:20 hrs, the elbow failed catastrophically due to the internal pressure exceeding the reduced strength of the pipe wall. This resulted in a high-pressure release of LPG, modeled as a full-bore rupture directed downwards at 45 degrees, with an initial flow rate of 133 kg/s. A large, dense vapour cloud quickly formed, expanding rapidly; modeling suggested a maximum flammable cloud volume of 10,000-15,000 cubic meters, reaching approximately 175m in length and 80m in width within seconds. Between 20 and 30 seconds after the initial release, the cloud encountered an ignition source, identified by the HSE investigation as likely being a fired furnace located 65m away. This triggered a massive VCE, with calculated overpressures reaching up to 0.5 bar within congested areas of the plant. The resulting blast wave caused immediate and severe damage across the SGP and adjacent areas, shattering windows and damaging structures both on and off site. A large fire erupted instantaneously, engulfing the SGP. The intense heat from this fire impinged on other nearby pipework and equipment. Approximately 10-15 minutes after the initial explosion (around 14:35-14:50 hrs), this heat exposure caused secondary failures (domino effects) in other pressurised systems due to material weakening. These subsequent releases fed the fire further, resulting in additional fireballs and increasing the overall intensity and scale of the blaze. The site emergency response team, supported by public fire services (Humberside Fire Brigade) and firefighters from the adjacent Lindsey Oil Refinery, responded promptly. The fire was brought under control by approximately 15:30-15:40 hrs (within about 70 minutes of the explosion). Efforts focused on isolating fuel sources by manually closing valves where possible. The fire was largely extinguished by 17:10 hrs and officially declared “struck out” by the fire brigade at 21:01 hrs.

  • Failure Mechanism Deep Dive (Erosion-Corrosion): The failure mechanism was definitively identified as erosion-corrosion occurring internally at the failed elbow. The carbon steel pipework (P4363) normally relies on a protective passive layer of iron sulphide (FeS) forming on its internal surface in the presence of corrosive species like H2S within the process stream. This layer significantly slows down the rate of general corrosion. However, the introduction of the continuous water wash, injected without a dispersion quill just upstream of the 90-degree elbow, fundamentally altered the internal environment. The jet of water physically impinged on the inner wall of the elbow, particularly at the outer radius where flow direction changes and turbulence is highest. This mechanical action (erosion) continuously removed the protective FeS scale layer. Once the protective scale was removed, the underlying bare carbon steel was directly exposed to the corrosive components (H2S, ammonia, chlorides) in the high-temperature, high-pressure gas stream. This led to rapid localized corrosion. The synergistic combination of mechanical erosion removing the protective layer and subsequent chemical corrosion of the exposed metal resulted in a dramatically accelerated rate of wall thinning specifically at the point of impingement. Over time, this localized metal loss reduced the pipe wall thickness from its original 7-8mm to less than 1mm, with a minimum recorded thickness of just 0.3mm. At this point, the pipe could no longer contain the internal operating pressure, leading to the sudden and catastrophic rupture.Â

  • Analysis of Management System Failures: The detailed analysis points to systemic failures rather than isolated errors. The MoC process failed critically when the water wash was introduced and later changed to continuous operation. It did not adequately identify or assess the significant erosion-corrosion hazard created by the modification, focusing instead on the intended operational benefit (fouling reduction). Using an existing vent point without proper engineering design (no quill, poor location) compounded the risk introduced by the change. The pipework inspection program was ineffective in detecting this specific failure mode. It likely relied on generic corrosion allowances or inspection intervals not suited for the localized, accelerated degradation occurring post-modification. The inspection strategy did not adequately target the high-risk area created by the water wash impingement near the elbow. Corrosion management practices failed to recognize or address the specific threat of erosion-corrosion in this context. Even if general corrosion was monitored, the localized mechanism driven by the water wash was overlooked or underestimated. Reports suggest that specific alerts about potential problems at injection points were not sufficiently acted upon. Communication breakdowns contributed significantly. The lack of effective information sharing about the change to continuous water injection prevented other groups (like Inspection or Engineering) from reassessing the risks or adjusting integrity management plans accordingly. Essential knowledge, potentially available from industry experience regarding this failure mechanism , was not effectively applied.Â

  • Mitigating Factors and Potential Severity: The most significant mitigating factor was the timing of the incident on a public holiday during shift change preparations, which drastically reduced the number of personnel exposed outdoors. Weather conditions (7.2 m/s northerly wind) influenced cloud dispersion, but modeling indicated that alternative wind scenarios were unlikely to have caused ignition at other potential sources or resulted in a significantly worse outcome, such as impacting the nearby HF Alkylation unit. Despite the low casualty count, the physical destruction clearly demonstrates the event’s massive energy release and catastrophic potential. The HSE explicitly stated the incident could have been far worse, drawing comparisons to the scale of the 1974 Flixborough disaster.

On March 23, 2005, a catastrophic explosion occurred at BP’s Texas City refinery in Texas, USA. The incident transpired during the startup of a hydrocarbon isomerisation (ISOM) unit. Operators inadvertently overfilled a raffinate splitter tower, causing it to flood with hydrocarbons. This led to the over-pressurisation of the tower and the release of a highly flammable hydrocarbon vapor cloud. The vapor ignited, resulting in a massive explosion that caused extensive damage across the refinery.

Date
23/03/2005
Location
United States of America
Industry
Energy (Oil Refining)
Substance
Hydrocarbons
Cause

The immediate cause was the overfilling of the raffinate splitter tower during startup, which led to the discharge of flammable liquid from the blowdown stack and its subsequent ignition.

Underlying causes were numerous and included:

  • Failure to establish effective safe operating limits.
  • Deficiencies in equipment design, including inadequate level indication, lack of automatic safety controls, and a blowdown system that discharged directly to the atmosphere without a flare. Previous tower overfilling incidents were not adequately addressed.
  • Inadequate startup procedures, including not removing liquid from the tower.
  • Inadequate shift turnover, leading to a loss of situational awareness.
  • Mechanical integrity deficiencies, including failures of critical instrumentation like the level transmitter (LT-5100) and a corroded high-level alarm float (LSH-5020).
  • Company safety culture, which lacked a focus on process safety management (PSM), encouraged cost-cutting over safety investments, and did not effectively respond to reports of serious safety problems.
  • Ineffective incident investigation system that failed to learn from previous blowdown incidents.
  • Poor placement of occupied trailers too close to the hazardous ISOM unit.
  • Insufficient operator training and the lack of supplementary assistance during the hazardous startup.
Consequence

The incident resulted in a major explosion and fire at the refinery. This led to:

  • 15 fatalities.
  • 180 injuries.
  • Significant financial losses exceeding $1.5 billion.
  • Alarm to the community.
  • Severe damage to the ISOM unit, surrounding parking areas, the satellite control room, and the catalyst warehouse.
  • Damage to over 40 trailers, with 13 destroyed.
  • Damage to approximately 70 vehicles.
  • Blast damage to buildings in surrounding units and off-site buildings.
  • Post-explosion fires.
  • Community shelter-in-place orders were issued in subsequent incidents at the refinery.
Injuries

180

Fatalities

15
All fatalities occurred in or near trailers located close to the ISOM unit.

Lessons Learned
  • Process unit startup is a significantly more hazardous period than normal operations and requires supplementary assistance and rigorous procedures. Incidents are significantly more likely during startups.
  • Blowdown systems discharging flammable materials directly to the atmosphere without a flare are inherently unsafe. Previous releases from the ISOM blowdown stack were early warnings that were not heeded.
  • Siting occupied trailers close to process units handling highly hazardous materials is extremely dangerous. Temporary structures are more susceptible to damage from explosions.
  • Reliance on low personal injury rates as a primary safety indicator can be misleading and fail to capture the risk of catastrophic process safety incidents. A focus on process safety metrics is crucial.
  • Deficiencies in mechanical integrity programs, including inadequate maintenance, testing, and calibration of critical instrumentation, can lead to failures with catastrophic consequences. Equipment data sheets must be kept up-to-date.
  • Effective incident investigation systems are essential for capturing lessons learned and implementing needed changes to prevent future incidents. Near-misses and previous incidents should be thoroughly investigated.
  • A strong safety culture with a focus on process safety management is paramount for preventing major accidents. This includes encouraging reporting of incidents without fear of retaliation and ensuring that management models and enforces safety procedures.
  • Organizational changes (MOC) must be systematically reviewed to ensure safety is maintained.
  • Board-level oversight and accountability for process safety are crucial.

Analysis

The incident at the BP Texas City Refinery on March 23, 2005, was a culmination of numerous safety system deficiencies and organizational failures. The startup of the ISOM unit’s raffinate splitter section involved filling the tower with liquid. However, the level control valve on the tower was not functioning correctly, and feed was added for approximately three hours without liquid being removed. Contributing to this was a malfunctioning level transmitter (LT-5100) that provided an inaccurate level reading to the control system. Additionally, a high-level alarm (LSH-5020) failed to activate due to a corroded float.

As the tower overfilled, pressure increased, causing three pressure relief valves to open. These valves discharged a large quantity of flammable raffinate liquid into a blowdown drum, which was designed to handle vapors and small amounts of liquid but quickly overfilled. The blowdown drum was connected to a stack open to the atmosphere and was not equipped with a flare to safely combust flammable releases. The overfilled drum resulted in a geyser-like release of flammable liquid out of the blowdown stack.

The cascading liquid from the stack atomized into small droplets, enhancing evaporation and the formation of a large flammable vapor cloud at ground level. The source of ignition is believed to have been a nearby idling pickup truck. The resulting vapor cloud explosion generated significant blast pressure that caused widespread damage and fatalities. Tragically, many contract workers were located in temporary trailers situated very close to the ISOM unit and the blowdown drum, and these trailers offered little protection against the blast.

The CSB investigation revealed that prior to this catastrophic event, there were numerous warning signs, including at least eight serious hydrocarbon releases from the ISOM blowdown stack between 1994 and 2004, some of which resulted in fires. Most ISOM startups also experienced high liquid levels in the splitter tower. However, these incidents were not effectively investigated, and lessons were not learned or implemented to prevent a recurrence.

Furthermore, the investigation highlighted a systemic lack of focus on process safety at the Texas City refinery, driven in part by cost-cutting measures and a prioritization of personal safety metrics over process safety management. Audits and studies had identified serious safety problems at the refinery for years, but the companies response was ineffective. The placement of the trailers near the hazardous unit, despite existing (though inadequate) siting policies and previous hydrocarbon releases, underscored a broader organizational failure to adequately assess and mitigate major accident risks.